A New Build

Now that the Bianchi is road-worthy, it’s time for the next project. A road bike, with a reasonably current frame, groupset, wheels, pedals, etc. Ultimately, the frame may be replaced with a different one – it could be carbon fiber (but probably not), or it could be a vintage lugged steel frame (much more likely).

But for now, the frame is a Cannondale CAAD8. It’s BBQ (flat black) with the full carbon premium Slice fork. In excellent shape, this should be a good starting point for the build.

The groupset is a 2010-11 full Campagnolo Veloce in black. I wanted the ultra-shift brifters, and the ultra-torque cranks and this was the best way for me to get those components.

I chose Boyd Vitesse wheels with 24F and 28R spoke counts.

The seatpost is an Alloy Fizik Cyrano, and the saddle is a Selle SMP Pro.

Here’s what I still need to decide on:

1. pedals
2. stem
3. handlebar

I’m going to stay with SPD-compatible pedals so that I don’t need to buy shoes AND pedals. I’m not racing the TDF, so the fact that they’re not purely road pedals is unimportant to me.

Once the Bianchi is completely dialed-in, I will take some measurements and that should take care of the stem decision.

If things progress as expected, I should be taking the first ride sometime in April or May. Since I’ve never built a bike from components, this will be a learning experience along the way.

Follow along, and we’ll see how it goes.

Bianchi, the last task

Handlebar tape. I’ve been putting this task off, mainly because I wanted to be sure the brake levers were in the right place, and I was working on the stem – but that’s done now. I didn’t want to waste $15 worth of handlebar tape either.

I looked at some youtube videos and read about the process on the Park Tools site and decided that my lack of experience would be equally lacking tomorrow or the next day. Time to get this finished.

Got scissors, some yellow electrical tape, and the handlebar tape. From start to finish it took less than 10 minutes to do both sides. I started at the bottom and wrapped up towards the stem. It’s not perfect around the brake levers, but that’s OK. Sooner or later it will need to be replaced and hopefully I will do a better job then. Until then, it’s tight, pretty evenly wound, looks decent, and adds some padding that was sorely (quite literally) needed.

I guess the Bianchi is complete now. Today’s weather looks good, so I’m planning a lunch ride.

Bianchi – the first real ride

The handlebars were too low and I couldn’t raise them any further. So, I ordered a taller quill stem from Harris Cyclery. But it was too tall so I cut off 3cm and it is close enough for now. To remove any more stem will require a different bolt as I’m out of threads on this one.

It rides much better (as tested on the indoor trainer) and I ran through all positions on the front and rear derailleurs. Brakes are good, all bearings are good, time for a road test. The temps are in the mid-60s, and it’s dry. Time to go.

Well, it was only 10 miles, but that was all it took. The bike rides great, makes all the expected mechanical noises – whirrs, clicks, shifting noises, etc. but no bad noises. The only obvious change necessary at this point is a mirror of some kind – more a survival aid than anything else.

Tomorrow, weather permitting, I’ll go a different direction for another 10 miles or so.

Work on the Bianchi

The bike arrived and unfortunately there were a couple of shipping scratches. I’ll get those handled after the mechanical going-over is complete. The bike was in very good condition and the only obvious issue is that the tires/tubes won’t hold pressure for long. Well, they are 30 years old so I really shouldn’t be surprised.

Taking things apart to check the bearings and adjustments isn’t too difficult, but I wanted to use the correct tools for the job. I purchased tools to remove the freewheel, to remove and adjust the bottom bracket, to remove and adjust the wheel bearings, and the headset.

I had a good quality grease available, cleaning supplies too. The job went smoothly with the proper tools and soon it was just about ready to ride. I knew the tubes weren’t holding pressure for long so I picked up replacement tubes. When I took the tires off to replace the tubes, the tires were cracked and falling apart. I’m not sure why I thought a 30 year old tube needed to be replaced but a 30 year old tire would be fine. See, I do get smarter as I get older – but it’s a slow process. 🙂

Anyway, I replaced the tires with Panaracer RibMo 700Cx25s and they ride very well. I haven’t had them on wet pavement yet, but they have good traction and ride quality. I’m running them at 90psi front and 100psi rear. For looks, gumwall tires are better(at least on a bike of this vintage), but these are fine and I have no plans to replace them anytime soon.

I do like the ride of a nice lugged steel frame…

A new bike in the stable

Not a motor-powered one, a human-powered one. A very nice early 1980’s Bianchi Limited. Even though it is more than 30 years old, it is in nearly mint condition. I’ve wanted a nice steel framed bicycle and because smaller frames fit me best but are harder to come by, when this one showed up I didn’t hesitate.

This winter it will see a complete going-over and will be ready for next spring. To tell the truth, it may just see a few miles yet this year – weather depending.

Take a look at these photos – very nice for a 30 year old bicycle.

More two-wheeled adventures…

This time, without gasoline. That’s right, bicycling.

Last year, my wife and I bought new bicycles. Good, not great, Trek bikes from a very good shop in Oswego, Illinois. When I was in high school in upstate New York, it seemed like I spent entire summers on the bike with a friend named Steve George. Up and down the hills of upstate New York; long ago I lost count of the miles and hours we spent riding. The bicycling bug never actually left, just was dormant for a while.

We started going on rides around the house, and also on the Fox Valley and Gilman bike trails. It’s been a lot of fun and good exercise too. I have a old Fuji Dynamic 12 I bought many years ago that is in need of restoration, maybe that will become a winter project. Precisely which winter remains a mystery.

Anyway, I decided this year to ride more and it’s been great. We’re fortunate to live in the country so we can go on several nice rides right out of our driveway.

More to come…

BMW reassembly, part 5

Ah, the electrical work. What I need to do is fairly simple, just replace the switches for the abs disable and the 4-way flashers so that the new ones will mount in the Highway Dirt Bikes top clamp.

Actually, those were the easy ones, but a problem with the turn signals caused quite a delay.

I couldn’t get the turn signals to work properly. The right signal was fine, the left one wouldn’t flash at all and the indicator flashed quickly. I swapped bulbs from right to left as they looked fine, but the left side was still inop. I noticed that the dash illumination bulbs were flashing when the left signal should have been flashing, so I began to suspect a diode. Of course the diodes on the F650 are hidden inside the crankcase – not really but they are still tricky to get a hand on. Replacement diodes from BMW are $17 each, and that was just ridiculous. I had some 3W diodes that should work fine, so I soldered 1/4″ spade fittings and then shrink-wrapped them. I replaced the original diodes and unfortunately the left signal was still inop. OK, this is becoming annoying. I took the left rear signal apart, and it was fine. The left front however was not. One of the wires was not attached to anything. We are talking 12v here so it wasn’t likely to spark across space. I crimped the connector together with pliers to make a better mechanical and electrical connection and like magic the turn signals (and the flashers) are working. At least I have better diodes that aren’t working at their maximum capacity in place now.

I removed the oem heated grip switch because it simply wasn’t possible to use it with the aftermarket heaters. All I needed was a DPST center off switch, but I spent a good hour with the ohmmeter trying to work out a set of contacts that would give that result. Not to be found. So, I ordered a switch blank to cover the oem switch and a new mini rocker switch. Both arrived fairly promptly and the wiring was simple enough.

The grip heater elements are held onto the throttle tube and the shrink wrap with 3M adhesive and then the grips are glued on with JB Weld. Not bad, all assembled and working properly with my brand new switch.

You might think we’re ready to go now, but you’d be wrong. With the addition of the risers, the front brake line from the handlebars to the ABS block on the headstock is now too short to allow full-lock turns. I took the oem line off and went to the local custom bike shop to order a replacement 2″ longer. When it came back the fittings weren’t exactly the same angles, so the line had to be routed slightly different to the original. That difference was enough that the 2″ should have been 3″, but it wasn’t. Crap. I ordered a new line (the fittings are OK) and now I get to wait another 2 days before I can put the brake line back in and bleed the front brakes.

Such are the joys of customizing bikes. Stay tuned for the exciting conclusion…

BMW reassembly, part 4

Now that the suspension is sorted out, the final hurdle is the handlebars and the hand guards. I ordered a set of Ultimate hand guards from Highway Dirt Bikes, including mirrors and switches. I had also ordered a set of Protaper SE alloy handlebars in the CR high bend. After some disassembly and some trial fitting, it was obvious that some risers were necessary to give the handguards the clearance needed for full-lock turns. I got a set of Rox risers that seemed to fit the bill and swapped the top clamp for the BMW for one that would fit the Rox riser bolt pattern. Now the clearance was OK. I turned some 1″ extensions to make the bars longer so that the switch housings could be placed in their (roughly) original positions. Mechanically, everything fits.

Stay tuned for the electrical work. My favorite.

BMW reassembly, part 3

I found a pair of stainless Supertrapp mufflers on ebay, and knowing that I wanted a tool tube on the right side and a single muffler on the left, I bought them. It fits properly, but I need a pipe bent and swaged to connect the exhaust pipe to the muffler inlet. Off to Tuffy’s in Yorkville. About 20 minutes after I got there I had a connecting pipe in place that only needed clamps and it was done.

The front wheel bearings and seals were the work of a few minutes and they were done. Freezing the bearings and heating the hubs made it fairly simple. A big socket that just fit the outer race was a help too.

READY TO RIDE!

The first ride was a disappointment. The forks were stiff and the rear shock was very nice. I guess the extra preload I added with the slightly longer spacer was coming back to bite me. Oops. Can’t leave it this way – one of the advantages of pvc spacers is that they’re easy to cut. Mark volunteered his garage this time, so I headed up there and we cut 5/8″ off the spacers and buttoned everything back up. Much better. After a few more miles I may still shorten the spacers a bit more, but I need to see how the forks work when the fluid is warmed up and on varying terrain.

There is a very large field north of my house that’s just begging to be ridden. The full knobby tires are very nice when you run into mud, the bike just keeps going, albeit more slowly than before. With the scorpions on the KTM, it would have been dirtnapping long before I ran out of mud.

Clearly, I had the wrong tires for the eastern TAT. Oh, well. Ride, pick up your bike in the mud, and learn.

I try.

BMW reassembly, part 2

OK, we’re finally back to a rolling chassis, or something pretty close to that. But the front wheel needs new bearings, seals, and axle spacers and the forks need Racetech valves, new springs, and new fluid. Luckily, my good friend Mark is up for the messy job of rebuilding the forks. Actually, it was Mark that made a mess by squirting fork oil on the ceiling of the garage. He’ll deny it but it’s still true.

Removing the front wheel and caliper is a few minutes work, and the forks are off a few minutes after that. Disassembly is almost always easier and quicker than reassembly – in my experience anyway. So we remove the circlips and the fork cap (not threaded on these forks) and pour out what fluid we can. The spacer and spring come out, along with a washer or two. The other fork was left assembled so that we would have a guide if our memory turned out to be faulty, or if our memory was so feeble that we couldn’t remember if it was faulty. Anyway, the piece of tubing supplied with the Racetech springs was not long enough to make spacers for both forks, so off to the hardware store we went. A piece of 1″ PVC tubing fits inside the forks, so that’s what I decided to use. I had to use my impact wrench to remove the bottom screw on the fork and finish the disassembly. While the forks are apart I replaced the bushings and guides.

We drilled the required holes in the tubing, cleaned the fork parts thoroughly, and began reassembly. About 10 minutes later, we had the fork reassembled and were ready to cut the spacer. From the top of the tube (while extended) to the bottom of the installed fork cap was about an inch of preload. We poured in 610ml of 10-wt Honda fork fluid. I left the spacer extending about 3/8″ out of the tube for 1 3/8″ of preload. The extra preload made it a booger to get the fork caps reinstalled but we got it done. The second fork was fairly simple having just seen the necessary steps. There was barely enough fork fluid for both, but we got the full 610ml in the second fork as well.

I replaced the stem bearings while the forks were out, as they seem to have a nasty habit of failing at around 20k miles and my F650 has, well, about 20k miles. Better to work on it here in the garage with a full set of tools than on the side of the road in BFE. Using the freezer and a heat gun, the job was actually pretty simple and the special socket for the special nut was helpful. I’ll put a few miles on it and then recheck the nut for the proper torque.

Next, the ride.